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#21
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In message
, John B writes I don't think that's true. The track layout at CULG implies that the through platforms aren't reversible: http://www.davros.org/rail/culg/picc...ayout...giving you 1 reverser at a time instead of 3 at Cockfosters. It is quite possible to have 3 reversers (east to west) at the same time at Arnos. Only platform 2/3 can reverse west to east though. -- Steve Fitzgerald has now left the building. You will find him in London's Docklands, E16, UK (please use the reply to address for email) |
#22
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#23
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On Jan 7, 10:14*pm, Stuart wrote:
wrote: "a stalled train at cockfosters" whatever the hell thats supposed to mean. How can you not understand what that means? Its very difficult to stall an electric motor so it won't turn and impossible to stall a dozen of them simultaniously. Its basically another LU buzzword bingo catch all phrase for a buggered up train which could be anything from sized brakes to it becoming gapped and it tells us nothing. Why they can't just say its broken down instead of trying to sound in-the-know when they probably don't have a clue by using a word such as stalled is anyones guess. B2003 |
#24
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![]() "John B" wrote in message ... On Jan 6, 1:52 pm, wrote: 1) the depot is at Cockfosters. Not sure what time this incident took place, but if the train died in a place where it blocked or MId to late afternoon. Right boys n' girls, this is what happened... (I have simplified this a bit but it's still gonna' be long) At about 14:53 a train departed CK platform 4, as it got out of the platform it became rear-tripped, coming to a halt with the rear of the train about 2 metres out of the platform. The T/Op went through his checks and identified the problem. He then set about getting the train moving. Sadly this is when it went all man-boobs up. The train had come to a stand on the one bit of track leaving CK where it was completely off juice (gapped in LU jargon) AND where the train will not roll - in either direction. Because the train was gapped the compressors were not working, and with the rear trip being operated (air escaping from the pressure switch) and several attempts to get the brakes to release, the available air on the train dropped below 3 bar at which point the train was not going to move no matter what unless it got back onto traction current. The SOP for this situation used to be to get a set of gap jumper leads (basically a 640 volt extension lead, with a plug to go into the side of the train on one end and a pair of shoes to go onto an adjacent possie and neggie rail on the other) that were stored locally to where trains could be gapped. Sadly LU's reading of the electricity at work act coupled with the current elf n' safety fetish has meant that gap jumpers have been deemed to be a BAD THING and have been removed from the majority of sites where we used to have them just in case someone who doesn't know what their doing tries to play with them. So, we've got a train sitting just outside CK preventing any other train going west from CK. We can get eastbound trains into P1 and P2/3 but the only place they can go after that is into the depot. (Which is what we did with the 3 trains that were stuck in section between OK & CK.) We can reverse trains at WG, AG & OK (which is what we did). The Arnos DMT drove up to CK, along with Tubelines staff from CFDT and station staff, but despite our best efforts we were unable to move the train. The ERU (Emergency Response Unit) had also been summoned and they were diverted to fetch the one set of gap jumpers known to be available. These were at Golders Green, the ERU were coming from Vauxhall so we ain't talking instant response here. Whilst this was going on, the customers on the stalled train expressed a desire to get off and continue their journey by other means, which, given that they had now been sitting there for 45 minutes was not unreasonable. So we got everyone into the car closest to the platform, cleared any trains between AG and OK, knocked the juice off, SCDs down, out with the train's detrainment ladder, walked the 15 customers off the train and onto CK platform, SCDs up, detrainment ladder back up and juice back on. The juice was off from 16:04 to 16:10. The current section runs from Cockfosters to Southgate, so we lost the OK reversing facility whilst the detrainment took place. This translated into about a 20 minute period that we had no trains running between AG and OK. Up until the detrainment we had been reversing at the 3 sites available to us. Once the detrainment had been completed we resumed OK reversing whilst we waited for the ERU to turn up with our jump leads. The ERU arrived on site at 17:05, we got the jump leads to the train. At this point we had to again get some trains out of section and so discharged TC at 17:15, deployed the jumpers, recharged at 17:20. We then had to let the air on the train build up, moved the train forward the 2 feet required to get it back on juice, knocked the juice back off at 17:30, removed the jumpers, juice back on at 17:35, train on the move at 17:36, delay 167 minutes. Whilst all this was going on, a track failure at Wood Green meant that we lost the WG reversing facility from about 16:30 onwards. The various discharges of traction current meant that we were not able to reverse at Oakwood from about 16:00 to 16:20 and from 17:10 to 17:40. So, Mr. B, I'm sorry that for you "Normal Crap Service" was resumed, we didn't do it deliberately and believe it or not some of us do care. If you want to get a chuckle out of the whole sorry saga, when I said that the Arnos DMT drove to CK, that man was me, only problem is I had not driven a car since 1990, so you can comfort yourself with thought that at least one of the bone idle useless layabouts who work for LU was actually sh*tting himself. Disclaimer: All opininions are my own. -- Cheers, Steve. Change jealous to sad to reply. |
#25
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On Jan 9, 3:38*am, "Steve Dulieu"
wrote: "John B" wrote in message ... On Jan 6, 1:52 pm, wrote: 1) the depot is at Cockfosters. Not sure what time this incident took place, but if the train died in a place where it blocked or MId to late afternoon. Right boys n' girls, this is what happened... (I have simplified this a bit but it's still gonna' be long) At about 14:53 a train departed CK platform 4, as it got out of the platform it became rear-tripped, coming to a halt with the rear of the train about 2 metres out of the platform. The T/Op went through his checks and identified the problem. He then set about getting the train moving. Sadly this is when it went all man-boobs up. The train had come to a stand on the one bit of track leaving CK where it was completely off juice (gapped in LU jargon) AND where the train will not roll - in either direction. Thanks for the comprehensive explanation (which I won't repeat). The bit I don't understand is how a whole train can be gapped. Could you clarify how that can occur (and why it isn't avoided for that matter)? How many shoes need to be in contact for movement to be possible, compressors to work etc? |
#26
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On Jan 9, 3:38*am, "Steve Dulieu"
wrote: gapped. Sadly LU's reading of the electricity at work act coupled with the current elf n' safety fetish has meant that gap jumpers have been deemed to be a BAD THING and have been removed from the majority of sites where we used to have them just in case someone who doesn't know what their doing tries to play with them. Thats just bloody dumb. I suspect even the nappy wearers at the H&SE would assume that an electric railway sometimes requires people to work with electricity! Someone in LU management needs a kicking. These were at Golders Green, the ERU were coming from Vauxhall so we ain't talking instant response here. Words for once fail me. The various discharges of traction current meant that we were not able to reverse at Oakwood from about 16:00 to 16:20 and from 17:10 to 17:40. If the announcements had just said that the power supply had to be switched off to detrain passengers instead of just saying "stalled train. the end" all would have been explained. Arnos DMT drove to CK, that man was me, only problem is I had not driven a car since 1990, so you can comfort yourself with thought that at least one So i'm guessing you don't own a car and had to borrow one so why didn't the owner of the car drive up there? I won't ask about insurance ![]() of the bone idle useless layabouts who work for LU was actually sh*tting himself. Look at it from a passengers point of view stuck in a tunnel yet again north of finsbury park with no information. Lets be honest , its not the first time this has happened. In the end me and the wife ended up getting a train back southbound to finsbury park to catch FCC which by then was offering a once every 20 mins service. Ended up at new southgate (no service on the hertford north line it appeared) and waiting in the cold for a 382 bus for another 20 mins which then proceeded to go around every damn side street it could find. Ended up taking not far off 2 hours to get home from central london. It only takes 3 hours to walk it! (I had to do just that on 7/7). Anyway , I take back what I said about LU staff. It seems your knob headed management caused this by removing all the gap leads. Bunch of ****s. B2003 |
#27
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In message of Fri, 9
Jan 2009 03:38:34 in uk.transport.london, Steve Dulieu writes Thanks for a REALLY interesting posting. It would do no harm for the TfL website to have similar reports for those few customers interested. (Pleasedon't count this as top-posting). "John B" wrote in message ... On Jan 6, 1:52 pm, wrote: 1) the depot is at Cockfosters. Not sure what time this incident took place, but if the train died in a place where it blocked or MId to late afternoon. Right boys n' girls, this is what happened... (I have simplified this a bit but it's still gonna' be long) At about 14:53 a train departed CK platform 4, as it got out of the It took me a while to be confident that CK means Cockfosters. You use several other two letter station codes. Where is the set publicly available? [snip] The T/Op went through his checks and identified the problem. He then Presumably Train Operator or driver in normal parlance, but planes are driven by pilots and ships by helmsmen. The train had come to a stand on the one bit of track leaving CK where it was completely off juice (gapped in LU jargon) AND where the train will not roll - in either direction. I presume that is a bit of track where most carriage lighting vanishes. (I guess residual lighting comes from batteries.) Why are such gaps needed? [snip] The SOP for this situation used to be to get a set of gap jumper leads Standard Operating Procedure CK.) We can reverse trains at WG, AG & OK (which is what we did). Wood Green, Arnos Grove and Oakwood. The Arnos DMT drove up to CK, along with Tubelines staff from CFDT and District Manager (Trains)? Completely Fouled Dam Trains? [snip] Whilst this was going on, the customers on the stalled train expressed a desire to get off and continue their journey by other means, which, given that they had now been sitting there for 45 minutes was not unreasonable. So we got everyone into the car closest to the platform, I love that summary of the customers' perspective. Was the driver able to use announcements for customer communication during the whole of the incident to this point. cleared any trains between AG and OK, knocked the juice off, SCDs down, SCD? discharged TC at 17:15, deployed the jumpers, recharged at 17:20. We Train Current? "discharged TC" = "switched track power off"? then had to let the air on the train build up, moved the train forward the 2 feet required to get it back on juice, knocked the juice back off 0.6m? So, Mr. B, I'm sorry that for you "Normal Crap Service" was resumed, we didn't do it deliberately and believe it or not some of us do care. If you want to get a chuckle out of the whole sorry saga, when I said that the Arnos DMT drove to CK, that man was me, only problem is I had not driven a car since 1990, so you can comfort yourself with thought that at least one of the bone idle useless layabouts who work for LU was actually sh*tting himself. Is the ability to drive a car part of your job? Should it not be exercised formally and regularly? You are plainly too valuable a member of staff to risk as described. (Not to mention elfin safety.) Could a C.S.A. (Customer Service Assistant) have been your driver? The 40 minutes you would have had to budget to travel by 298 bus is probably excessive. A Taxi account would probably be better. On the other hand, I am sure stress probably affected those dealing with the situation. Disclaimer: All opininions are my own. 2 obvious questions: 1) Was there train operator error? 2) Should jumper availability be reviewed? e.g. Put them in a locked cupboard with a notice indicating the criteria for opening the cupboard. The expected return period of such a cost (delay in powering the train) would have to be balanced against the cost of more availability. Thank you again for a REALLY interesting report. Thanks to Boltar for THIS thread that stimulated your response. -- Walter Briscoe |
#28
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On Jan 9, 11:24*am, Walter Briscoe
wrote: 2 obvious questions: 1) Was there train operator error? 2) Should jumper availability be reviewed? e.g. Put them in a locked cupboard with a notice indicating the criteria for opening the cupboard. The expected return period of such a cost (delay in powering the train) would have to be balanced against the cost of more availability. Wonder if it would be possible to have some sort of creep mode that would work off the train batteries that could move it forward a couple of metres at a crawl on level ground. It would probably drain the battery in seconds but would solve gapping issues if the bedwetters have decided gap leads are too dangerous to be used. B2003 |
#29
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![]() "MIG" wrote in message ... On Jan 9, 3:38 am, "Steve Dulieu" wrote: "John B" wrote in message ... On Jan 6, 1:52 pm, wrote: 1) the depot is at Cockfosters. Not sure what time this incident took place, but if the train died in a place where it blocked or MId to late afternoon. Right boys n' girls, this is what happened... (I have simplified this a bit but it's still gonna' be long) At about 14:53 a train departed CK platform 4, as it got out of the platform it became rear-tripped, coming to a halt with the rear of the train about 2 metres out of the platform. The T/Op went through his checks and identified the problem. He then set about getting the train moving. Sadly this is when it went all man-boobs up. The train had come to a stand on the one bit of track leaving CK where it was completely off juice (gapped in LU jargon) AND where the train will not roll - in either direction. Thanks for the comprehensive explanation (which I won't repeat). The bit I don't understand is how a whole train can be gapped. Could you clarify how that can occur (and why it isn't avoided for that matter)? How many shoes need to be in contact for movement to be possible, compressors to work etc? You need one positive and one negative shoe on current. Because of all the point work at CK there are numerous gaps in the juice rails. Had the train stopped two feet in either direction it would not have become gapped. -- Cheers, Steve. Change jealous to sad to reply. |
#30
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![]() "Walter Briscoe" wrote in message news ![]() In message of Fri, 9 Jan 2009 03:38:34 in uk.transport.london, Steve Dulieu writes Thanks for a REALLY interesting posting. It would do no harm for the TfL website to have similar reports for those few customers interested. (Pleasedon't count this as top-posting). "John B" wrote in message ... On Jan 6, 1:52 pm, wrote: 1) the depot is at Cockfosters. Not sure what time this incident took place, but if the train died in a place where it blocked or MId to late afternoon. Right boys n' girls, this is what happened... (I have simplified this a bit but it's still gonna' be long) At about 14:53 a train departed CK platform 4, as it got out of the It took me a while to be confident that CK means Cockfosters. You use several other two letter station codes. Where is the set publicly available? Not sure that there is a publicly available set, sorry... [snip] The T/Op went through his checks and identified the problem. He then Presumably Train Operator or driver in normal parlance, Correct... The train had come to a stand on the one bit of track leaving CK where it was completely off juice (gapped in LU jargon) AND where the train will not roll - in either direction. I presume that is a bit of track where most carriage lighting vanishes. (I guess residual lighting comes from batteries.) Why are such gaps needed? Correct, gaps are to allow for points, section isolation, current section change overs... [snip] The SOP for this situation used to be to get a set of gap jumper leads Standard Operating Procedure CK.) We can reverse trains at WG, AG & OK (which is what we did). Wood Green, Arnos Grove and Oakwood. Correct... The Arnos DMT drove up to CK, along with Tubelines staff from CFDT and District Manager (Trains)? Completely Fouled Dam Trains? Duty Manager Trains. CockFosters DepoT... [snip] Whilst this was going on, the customers on the stalled train expressed a desire to get off and continue their journey by other means, which, given that they had now been sitting there for 45 minutes was not unreasonable. So we got everyone into the car closest to the platform, I love that summary of the customers' perspective. Was the driver able to use announcements for customer communication during the whole of the incident to this point. Yes... cleared any trains between AG and OK, knocked the juice off, SCDs down, SCD? Short Circuiting Device, basiclly a big metal bar with a magnet on each end that you put across the juice rails once TC has been discharged and you want to move about in a safe area on the track. Should TC be recharged inadvertantly the SCD causes a circuit breaker to operate which knocks the juice off again... discharged TC at 17:15, deployed the jumpers, recharged at 17:20. We Train Current? "discharged TC" = "switched track power off"? Traction Current and correct... then had to let the air on the train build up, moved the train forward the 2 feet required to get it back on juice, knocked the juice back off 0.6m? Yup... So, Mr. B, I'm sorry that for you "Normal Crap Service" was resumed, we didn't do it deliberately and believe it or not some of us do care. If you want to get a chuckle out of the whole sorry saga, when I said that the Arnos DMT drove to CK, that man was me, only problem is I had not driven a car since 1990, so you can comfort yourself with thought that at least one of the bone idle useless layabouts who work for LU was actually sh*tting himself. Is the ability to drive a car part of your job? Should it not be exercised formally and regularly? The ability to drive is not actually part of the job description, I hold a valid driving license, however I don't own a car myself. The vehicle was the Arnos Grove incident response vehicle (a white and blue Zafiera with flashing orange lights on the top) which all DMTs are insured to drive. At the time of the incident I was the only person available to drive it so it was a case of gird loins, deep breath and off we go. Any spare station staff floating about were down at Finsbury Park for the footie at Arsenal. In actual fact, the drive up to Cockfosters was not too bad, nice bright sunny day and not much traffic. Getting the car back was a bit of a bugger though, dark, bloody cold and of course I'm trying to get it out of Cockfosters car park along with god knows how many Gooners following the match at Arsenal. You are plainly too valuable a member of staff to risk as described. (Not to mention elfin safety.) You are too kind... Could a C.S.A. (Customer Service Assistant) have been your driver? The 40 minutes you would have had to budget to travel by 298 bus is probably excessive. A Taxi account would probably be better. On the other hand, I am sure stress probably affected those dealing with the situation. We have a Taxi account, however it would have still taken a good 30-40 minutes to get a cab so the response vehicle was the prefered option. Disclaimer: All opininions are my own. 2 obvious questions: 1) Was there train operator error? No... 2) Should jumper availability be reviewed? e.g. Put them in a locked cupboard with a notice indicating the criteria for opening the cupboard. The expected return period of such a cost (delay in powering the train) would have to be balanced against the cost of more availability. Well personally I think it's a spectacularly dumb idea not to have them available, but then having spent over two hours freezing my gribblies off up at Cockfosters on Saturday I suppose I'm biased. Had they been available the train would have been moving in about 30 minutes rather than 167. I suspect that cost as much as anything is behind the decision to remove them, they require periodic testing (not cheap) and any staff using them would need training and annual refresher training (really not cheap). Thank you again for a REALLY interesting report. You're most welcome... Thanks to Boltar for THIS thread that stimulated your response. -- Cheers, Steve. Change jealous to sad to reply. |
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